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3 Aug 08
5 Aug 08
Some time ago, Bachmann added a railtruck to
their Spectrum line. railtrucks were adaptations of highway vehicles
intended to reduce the cost of operations on lightly traveled lines.
This was a desperation move by the railroads in an attempt to stave off
bankruptcy a little longer. Eventually, however, the inevitable
happened and the rail lines had to shut down. They just could not
compete with cars and trucks after a suitable road system had been
built out. Most of these rail vehicles were one of a kind contraptions
built in the railroad's own shops. This one is a stakebed truck used to
continue the mail contracts. It is lettered as RGS No. 1.
The detail on this model is quite
good. Bachmann has gone to great lengths to produce a sturdy and good
looking model. The scale is nominally 1:20.3. Even the mechanical
layout is reasonably close to the prototype. The hood panels can be
lifted to reveal an engine. The motor is under the hood inside the
shell of the engine model. One shaft of the motor is used to drive the
engine's fan. The cab is detailed with a seat, a driver (packaged
separately) and some controls such as a gearshift lever. Under the
floorboards is a gearbox where the transmission would normally be. The
rear axle is driven via a functional drive shaft.
The bed has a large box in the middle which is used to house the electronics. There are yellow LEDs in the headlights which simulate the normally weak 6 volt electrical system of these vehicles and there is a single red LED to the rear required by railroad practice. The electronics has an interface for a DCC decoder and provides reasonable constant intensity lighting when driven by Aristo's Train Engineer with PWC. The constant intensity lighting doesn't do nearly as well with linear power.
The running properties, however, were not so good, at least on the one that I bought. It ran fairly quietly in reverse, but made rather bothersome noises running forward as can be heard in this short H.264 movie clip of the railtruck as delivered. You'll need something like QuickTime that can decode H.264 to view the clips on this page.
On downgrades the railtruck has a serious surge as the slack in the drive train is repeatedly taken out and then builds up again. The surging is not nearly as bothersome to me as the grinding sound made by the gearbox. It sounded bad and had to be investigated before I could put any significant runtime on the railtruck.
Further, there is a gear alignment problem that would certainly result in early gear failure.
Power pickup seemed to be pretty good even though I found that one of the rear wheels did not pick up power, see a separate section below concerning this other manufacturing problem. Even before the power pickup fix, it was pretty reliable. After the fix it was quite good, I detected no tendency to stutter or stall at all on my indoor track, which is in good condition.
The railtruck handles 4 ft diameter curves (LGB R1) with no difficulty except for only a little slowing in the curves. However, it could not handle the 2 ft diameter curves on my trolly line. This should not be an issue as hardly anybody but me is crazy enough to bend track that tight.
Tracking is excellent. After some high speed running in both directions all over the GIRR Mountain Division, the railtruck didn't derail at all. Running backwards, it did consistently pick the point of one turnout, but that was the turnout's fault. A little work with a grinding wheel at the offending point fixed that problem completely.
I had heard that Dave Goodson at NorthWest Remote Control Systems had worked up a procedure for fixing a systematic manufacturing defect that afflicts part or all of the initial railtruck production. He sent me these instructions, which I followed and documented below. Even though my unit did indeed have this particular problem, Dave's fix didn't impact the running noise. Dave's fix, however, will likely prevent the railtruck from eating it's own gearing.
The basic problem is that the output gear is not properly constrained due to some incorrect screws (or perhaps due to tapped holes that are too shallow) and the meshing of the gearbox output bevel gear is uncontrolled.
Dave's instructions are in italics:
The final drive surge is single-lead worm related, and slack in
those u-joints. No real economical fix.
Dave
31JAN2006
Tearing down 5 new Railtrucks (3 here, 2 at Barry's), we have
discovered an issue which in most probability will result in failure of
the output gears in the transmission (gearbox) of this unit.
The screws in question (from the parts breakdown list provided with the unit) are Kader Part Number SCREW-10644.
These are about .195" in length from under the head to end of threads. They need to be no longer than .150", and probably for manufacturing tolerances, about .140".
The screws are bottomed out in the holes. This prevents the keeper (Kader 00L06, I think it says) from holding the brass bearing firmly in the housing, allowing extreme wobble and gear un-mesh in the output bevel gears, which shall result in failure at some point.
Procedure:
As an addendum:
The screws provided with the snowplow are exactly the correct
length.
We are still working on the surging on grades, two paths in work at this time.
TOC
Published with permission of Bachmann Industries. This notice must be attached to any copies.
Following is a photo narrative describing my experience in making this modification. It is not difficult to do at all. The only tool that is needed is a Phillips jeweler's screwdriver although a Kadee 5-finger grabber tool is handy for holding the very small screws.
The stakes and engine cowls
come off easily with a small amount of flexing. The side stakes are
secured to the rear of the cab by small tabs. Simply flex the cab away
from the side stakes just a little to release the tabs.
There is one screw down inside the box on the truck bed that has to come out. It is pointed to by the screwdriver in the photo. The bed box has to be able to flex upward to clear the mounting tabs for the cab so that the cab can be removed. It is safe to gently pull the front of the bed box upward while removing the cab to clear these tabs.
The cab is released by removing
two screws underneath. One is visible, the other is hiding in the
shadow of the muffler. These screws engage lugs on the rear of the cab
that would interfere with the bed box if that one screw in the bed box
was not removed.
The two flathead screws in
the cab floor hold the floor down. The cab floor is also the top cover
of the gearbox, our objective.
This is
the gearbox. The offending screws are the in lower part of the picture,
just to the right of center. If your railtruck has a screw problem, the
keeper piece will be loose as the longer screws have bottomed out
without bearing down on the keeper.
If the railtruck is run with a loose keeper, the bevel gear leading to the driveshaft will squirm around as the direction of the railtruck is shifted from forward to reverse. The imprecise position of this bevel gear will result in early failure if it is not fixed. The shorter screws supplied with the snowplow are indeed just right. Since I wasn't planning on using the snowplow anyway, it was obvious that a swap for the longer screws was the hot setup.
Note that the cab can fit back on in two ways. In the incorrect way, it sits a little too far to the rear and the hood pieces do not fit properly. If you find this problem, lift the cab and reinstall it in the most forward position that it will fit.
When I completed this fix and retested the railtruck, the noise problem was not changed as can be heard in this clip. The problem is at the motor worm. There appears to be a thrust oscillation in the motor shaft which is resulting in the noise. After I determined that the noise wasn't going to cause the gearing to self destruct immediately, I ran it for awhile and the noise reduced, but it had not gone away in a few minutes running.
If I press on the end of the worm while the railtruck is moving forward, the oscillation is damped and the noise goes away. If I lift the drive wheels from the track to remove much of the load on the drive train, the noise also goes away. If I push the railtruck forward lightly while is running slowly forward to remove the load on the drive train, the noise also goes away. When the railtruck is running downhill and it is lightly surging, the noise follows the surge. When the drive train slacks due to the surging, the noise stops.
It turned out that all it needed was some more significant run-in time to get the gearing to wear together properly. This clip shows what about an hour of running did.
The Bachmann Railtruck is susceptible to surging due to the accumulated slop in the driveline. There is a total of about a quarter drive wheel turn of play in the overall driveline all the way back to the worm. The worm itself is a single lead screw which cannot be backdriven. When running on the flat, or with a load, the slop is all taken up and the railtruck runs smoothly. However, when running downgrade, the driveline doesn't provide enough drag and the railtruck runs away due to the pull of gravity until the slop is all taken out and the driveline binds up against the worm. As the worm gear continues to turn, it drives the railtruck downhill and runs the slop out the other way until the acceleration of gravity takes over again and the railtruck runs ahead of the worm again. The surging due to the driveline slop can be seen in this short clip.
If a loco is placed on a grade and pushed back up until the wheels slip and it can then roll downgrade from there, it will surge to some extent on that grade. Possible solutions take two diverging paths, either the backlash has to go or the tendency to free roll has to go.
I spoke with Barry of Barry's Big Trains at the Big Train Show yesterday and he says that he has completely reworked the driveline to eliminate the slop and therefore the surging. Contact him for details.
If there is enough drag such that the railtruck cannot free roll on a downgrade, then it can't get ahead of itself and it won't surge. This can be seen in the clip when the railtruck enters the curve where the drag increases and the surging immediately stops.
Adding drag is an inelegant hack but
it can be easily kludged and it does work as shown in this clip. I found a
piece of 0.032" x 0.250" brass strip on my workbench and I bent a piece
to act as a spring bearing against the front axles. I had originally
intended to hold it in place with the screw on the truck, but the screw
was too short and I didn't have a longer one with the same thread.
However, I found that the strip will hold itself in place just fine. It
can be placed anywhere along the axles. The tension on the spring is
somewhat critical. Too much pressure and the front wheels will not
turn. Too little and the railtruck will still surge, but there is a
sweet spot that allows the wheels to rotate and still provides
sufficient drag to stop the surging. A technically better place to add
drag would be at the rear axle, but an easy way to implement that
feature there hasn't occurred to me.
With this simple and reversible modification, the railtruck doesn't surge on my 4% grades at any speed and it still runs smoothly and quietly.
As part of my usual locomotive
testing process, I lift all the wheels but one axle's worth, one axle
at a time, from the track to be sure that all of them are picking up
power. On this model, the rear wheels did not pick up power. I quickly
traced this to bad solder joints where the wires come down from the
electronics box to the wheel contacts. One contact has been removed in
this photo, it was the bad one. The other side also has a bad solder
joint, but it was at least making contact.
There are four screws at the corners of the rear axle structure that allow the whole rear end to be removed. It will simply slip out of the driveshaft. Upon reassembly, make sure that both ends of the driveshaft fix back into the universal joints.
The fix was a simple resolder job. However, the tabs are very lightweight metal and they sit in the plastic bed. If you just touch them with a regular soldering iron, you'll melt them right into the bed. First lift them off the bed surface a little with a toothpick and then use a very fine tip soldering iron at low heat and apply a very small amount of solder to make a reliable contact.
The wheel contacts themselves are
in a form that I have not seen before. They have very small rollers
that ride on the wheel back to reduce friction and noise. The power
pickups on the front wheels are the same design.
The rollers seem to work quite well. They do roll with the wheels, but there is a downside to this contact type. The roller is very small. Therefore it has to turn quite fast to keep up with the wheel. There isn't much spring tension holding it against the wheel, but there is some. Even with the light pressure, the high speeds will result in bearing wear unless the bearing is lubricated. The bearing is a simple pin, both the pin and the roller rotate so that the pin will wear both inside the roller and in the fork. If these surfaces are left unlubricated, I expect that the pins, rollers or forks will eventually completely wear through. This will happen with lubrication as well, but at a much slower rate.
Considering that the low drag contacts actually contribute to surging, Bachmann may have been better served by using conventional friction contacts.
I took the railtruck back to the outdoor GIRR and tried it. There hadn't been a train movement in three months (due to extended travel and building projects) and the track was pretty dirty. The railtruck sputtered. After several passes with a track cleaning car, the GP9 pulling it was still being impacted by the dirty track a little but the railtruck ran without a hitch, not a hint of sputter or even headlight flicker. It also ran on DCC (address 0) but it made the typical DCC hiss that all analog locos make while running at DCC address 0.
This is the
interconnection diagram for the Railtruck as configured for track
power. I did not try to tease out the wiring of the printed wiring
board as it appeared pretty simple and the information that I needed to
proceed with a sound installation was actually all on these drawings.
Also, the board doesn't come out easily so I couldn't get to the back
of it without tearing up too much wiring.
A full size PDF of this image is available at the link.
The PWB itself contains a bridge rectifier and filter capacitor to provide power to the headlights and tail light which are non-directional. It also provides the interconnection points for a DCC installation. This is important to me because track power is easily accessible on terminals 1 and 2. The black and red wires that are already there go to the motor, they will stay there when these points are used to drive a sound board.
For a DCC installation,
the red, black and blue wires are removed from terminals 1, 2 and 3 and
are instead wired to a decoder. The blue wire (on the board, not to be
confused with a decoder blue wire) is for the headlights which are
wired together internally. It is not easy to make them directional even
with a decoder. The black and red wires go to the motor output of a
decoder. The blue wire goes to the headlight outputs (both forward and
reverse) of a decoder. The red and black wires on the decoder (power
input) go back to terminals 1 and 2.
A full size PDF of this image is available at the link.
This wire
color stuff is confusing because it conflicts with the DCC standards.
The red and black wires that go from pads H and I to terminals 1 and 2
ought to be orange and gray. The blue wire that goes to terminal 3
ought to be white. In any event, to connect a decoder, these three
wires need to be spliced into decoder wires.
I have elected
to install a Soundtraxx Sierra Goose sound system in the railtruck.
This time around, I am resigned to using a smaller speaker. This one
came in the Climax Sierra that I installed in a Bachmann Heisler. In the Heisler, I
used a larger speaker as that sound system sounds better with it. The
goose sound doesn't have as much bass in the sound and it can get away
with a smaller speaker. Besides, there just isn't room for a larger
one.
I will build an L-shaped box that looks like two crates to enclose the speaker, battery and the Sierra. The Sierra itself will sit on top of the tool box. The Sierra is slight narrower and much shorter than the took box. The lid of the toolbox will be part of the sound system box. I'll run a pair of wires through the cover of the toolbox and put a two terminal connector inside the tool box so that the whole assembly can be removed. The sound system power switch will sit low to the floor facing rearward. Some black paint will make it less visible.
The battery is a 5 AAA NiMH set as the included Sierra gelcell battery is much too large.
Even
though the Sierra hasn't arrived, I went ahead and prepared the
speaker. I built up a styrene box and fashioned the visible sides to
look like a crate. I did the typical scrape with a razor saw and
blackwash tricks to simulate some wood grain.
I had originally intended to put the speaker and battery pack in the same box, then I though better of it. There would be too much weight on one side so the battery pack was rearranged slightly so that it would fit on the other side and not be so tall. The wires from the speaker fit between the cab and the tool box.
The face of
the speaker shows through the stakes. I need to find a scrap of thin
cloth about the same color as the crate to make a grill for it.
I haven't yet decided exactly how I am going to mount the Sierra, the power switch is the sticking point.
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This page has been accessed times since 2 Jun 08.
© 2008 George Schreyer
Created 2 Jun 08
Last Updated August 5, 2008